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This repository has been archived by the owner on May 3, 2021. It is now read-only.
Hello, I have 2 controllers and both of them have the same problem. When I pair them and I want to calibrate them using calibartion mat the controller turn off after few seconds. While running rumble test controller disconnects after ~3 seconds. Few days earlier I had a problem only with one of them but now anyone is not working. Everything is ok until I enter rumble test, color calibration, position calibration or steamvr. Gyroscope/magnetometer works as it should.
[2019-12-27`` 18:06:08.459]: main - Starting PSMoveService v0.9-alpha 9.0.1 (protocol v0.9-alpha 9.0.0) [2019-12-27 18:06:08.492]: USBAsyncRequestManager::startup - Requested LibUSBApi [2019-12-27 18:06:08.494]: USBAsyncRequestManager::startup - Creating LibUSBApi [2019-12-27 18:06:08.503]: USBAsyncRequestManager::startup - Initialized USB API [2019-12-27 18:06:08.514]: DeviceManager::startup - Platform Hotplug API is ENABLED [2019-12-27 18:06:08.564]: bluetooth_get_host_address - Found a bluetooth radio [2019-12-27 18:06:08.565]: bluetooth_get_host_address - Retrieved radio info [2019-12-27 18:06:08.616]: VirtualHMD::open - Opening VirtualHMD(VirtualHMD__0). [2019-12-27 18:06:08.625]: DeviceTypeManager::update_connected_devices - Device device_id 0 (VirtualHMD) opened [2019-12-27 18:06:25.870]: PSMoveController::open - Opening PSMoveController(\\?\hid#{00001124-0000-1000-8000-00805f9b34fb}_vid&0002054c_pid&03d5&col01#8&28703830&d&0000#{4d1e55b2-f16f-11cf-88cb-001111000030}) [2019-12-27 18:06:25.876]: PSMoveController::open - with serial_number: 000704a31206 [2019-12-27 18:06:25.958]: WorkerThread::start - Starting worker thread: PSMoveSensorProcessor [2019-12-27 18:06:25.964]: DeviceTypeManager::update_connected_devices - Device device_id 0 (PSMove) opened [2019-12-27 18:06:31.874]: ClientConnection::start - Starting client connection id 0 [2019-12-27 18:06:31.876]: ClientConnection::send_connection_info - Sending connection id to client 0 [2019-12-27 18:06:35.947]: ServerRequestHandler - Start controller(0) stream (pos=0,phys=0,raw_sens=0,cal_sens=0,trkr=0,roi=0) [2019-12-27 18:06:39.476]: ServerDeviceView::poll - Device id 0 closing due to no data (100 failed poll attempts) [2019-12-27 18:06:39.478]: PSMoveController::close - Closing PSMoveController(\\?\hid#{00001124-0000-1000-8000-00805f9b34fb}_vid&0002054c_pid&03d5&col01#8&28703830&d&0000#{4d1e55b2-f16f-11cf-88cb-001111000030}) [2019-12-27 18:06:39.483]: WorkerThread::stop - Stopping worker thread: PSMoveSensorProcessor [2019-12-27 18:06:40.124]: PSMoveSensorProcessor::doWork - HID ERROR: The I/O operation has been aborted because of either a thread exit or an application request. [2019-12-27 18:06:40.139]: WorkerThread::stop - Worker thread stopped: PSMoveSensorProcessor
The text was updated successfully, but these errors were encountered:
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Hello, I have 2 controllers and both of them have the same problem. When I pair them and I want to calibrate them using calibartion mat the controller turn off after few seconds. While running rumble test controller disconnects after ~3 seconds. Few days earlier I had a problem only with one of them but now anyone is not working. Everything is ok until I enter rumble test, color calibration, position calibration or steamvr. Gyroscope/magnetometer works as it should.
[2019-12-27`` 18:06:08.459]: main - Starting PSMoveService v0.9-alpha 9.0.1 (protocol v0.9-alpha 9.0.0) [2019-12-27 18:06:08.492]: USBAsyncRequestManager::startup - Requested LibUSBApi [2019-12-27 18:06:08.494]: USBAsyncRequestManager::startup - Creating LibUSBApi [2019-12-27 18:06:08.503]: USBAsyncRequestManager::startup - Initialized USB API [2019-12-27 18:06:08.514]: DeviceManager::startup - Platform Hotplug API is ENABLED [2019-12-27 18:06:08.564]: bluetooth_get_host_address - Found a bluetooth radio [2019-12-27 18:06:08.565]: bluetooth_get_host_address - Retrieved radio info [2019-12-27 18:06:08.616]: VirtualHMD::open - Opening VirtualHMD(VirtualHMD__0). [2019-12-27 18:06:08.625]: DeviceTypeManager::update_connected_devices - Device device_id 0 (VirtualHMD) opened [2019-12-27 18:06:25.870]: PSMoveController::open - Opening PSMoveController(\\?\hid#{00001124-0000-1000-8000-00805f9b34fb}_vid&0002054c_pid&03d5&col01#8&28703830&d&0000#{4d1e55b2-f16f-11cf-88cb-001111000030}) [2019-12-27 18:06:25.876]: PSMoveController::open - with serial_number: 000704a31206 [2019-12-27 18:06:25.958]: WorkerThread::start - Starting worker thread: PSMoveSensorProcessor [2019-12-27 18:06:25.964]: DeviceTypeManager::update_connected_devices - Device device_id 0 (PSMove) opened [2019-12-27 18:06:31.874]: ClientConnection::start - Starting client connection id 0 [2019-12-27 18:06:31.876]: ClientConnection::send_connection_info - Sending connection id to client 0 [2019-12-27 18:06:35.947]: ServerRequestHandler - Start controller(0) stream (pos=0,phys=0,raw_sens=0,cal_sens=0,trkr=0,roi=0) [2019-12-27 18:06:39.476]: ServerDeviceView::poll - Device id 0 closing due to no data (100 failed poll attempts) [2019-12-27 18:06:39.478]: PSMoveController::close - Closing PSMoveController(\\?\hid#{00001124-0000-1000-8000-00805f9b34fb}_vid&0002054c_pid&03d5&col01#8&28703830&d&0000#{4d1e55b2-f16f-11cf-88cb-001111000030}) [2019-12-27 18:06:39.483]: WorkerThread::stop - Stopping worker thread: PSMoveSensorProcessor [2019-12-27 18:06:40.124]: PSMoveSensorProcessor::doWork - HID ERROR: The I/O operation has been aborted because of either a thread exit or an application request. [2019-12-27 18:06:40.139]: WorkerThread::stop - Worker thread stopped: PSMoveSensorProcessor
The text was updated successfully, but these errors were encountered: